997 Turbo / GT2 2006–2012 Turbo discussion on the 997 model Porsche 911 Twin Turbo.
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Old Dec 7, 2013 | 12:06 PM
  #31  
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Nice to hear P.

I guess the boost must feel more instantaneous with the 3.8ltr and a lot more torque is produced without WOT.
 
Old Dec 7, 2013 | 12:33 PM
  #32  
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Originally Posted by K24F
WG set @0,8bar gives 1,2Bar! I did a few very short pulls in 4rth.
I will low to 0,6-7Bar tomorrow, I really don't understand this "story"?...
I'm having a similar problem

I think my wg is set to 0.95bar, with EBC off I get 1.15bar and with EBC set to 1.25bar I get 1.45bar

Since what happened to your engine i've been running with EBC off, I'm scared
 
Old Dec 8, 2013 | 02:07 AM
  #33  
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You have connected both something wrong. Pascal have you changed settings from Internal wg to external? You can both disconnect the top hoses on the wg's and only have the side ports to wg hooked up to the compressors on the turbos. Block off the lines coming from the wg solenoid, but be sure to leave the port on the top of the wg open for vent. This will run the lowest boost. (Or spring pressure) I have on my car .8 bar springs.

If you continue to have higher boost then you have installed wrong color springs in the wg.
 
Old Dec 8, 2013 | 02:55 AM
  #34  
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Originally Posted by w00zy
I'm having a similar problem

I think my wg is set to 0.95bar, with EBC off I get 1.15bar and with EBC set to 1.25bar I get 1.45bar

Since what happened to your engine i've been running with EBC off, I'm scared
Hi Rui,
You can set your HKS to the basic WG boost, if it is 1,15 EBC off so set 1,15 and the HKS will respect its targets.
 
Old Dec 8, 2013 | 03:02 AM
  #35  
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Originally Posted by Aisxos
You have connected both something wrong. Pascal have you changed settings from Internal wg to external? You can both disconnect the top hoses on the wg's and only have the side ports to wg hooked up to the compressors on the turbos. Block off the lines coming from the wg solenoid, but be sure to leave the port on the top of the wg open for vent. This will run the lowest boost. (Or spring pressure) I have on my car .8 bar springs.

If you continue to have higher boost then you have installed wrong color springs in the wg.
Hi Nick,
My springs are the Alpha's stock ones, and the pressure was ok with them and the old setup.
I checked all the hoses too, all are brand new, nice routed and not hurted.
I try the lowest boost possible this morning, each WG cracks about 0,75/80Bar, I go for a run now.
I believe the very free flow exhaust combined with the Cc increase is the reason,
perhap's I will have to swap my springs?...
 
Old Dec 8, 2013 | 03:10 AM
  #36  
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Originally Posted by K24F
Hi Nick, My springs are the Alpha's stock ones, and the pressure was ok with them and the old setup. I checked all the hoses too, all are brand new, nice routed and not hurted. I try the lowest boost possible this morning, each WG cracks about 0,75/80Bar, I go for a run now. I believe the very free flow exhaust combined with the Cc increase is the reason, perhap's I will have to swap my springs?...
This isn't the reason.. I have 4.1 engine with cat less 3inch exhaust and I don't face such a problem...
 
Old Dec 8, 2013 | 03:14 AM
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Hi Pascal,
several months ago i had very similar issue(overboost)the small filter connected to the hose going to the stepping motor(solenoid)of the HKS was partially closed.
 
Old Dec 8, 2013 | 09:06 AM
  #38  
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Originally Posted by Aisxos
This isn't the reason.. I have 4.1 engine with cat less 3inch exhaust and I don't face such a problem...
Exact, but did you rebolt the A3071 with your new setup?
 
Old Dec 8, 2013 | 09:10 AM
  #39  
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Originally Posted by dynamic gt2
Hi Pascal,
several months ago i had very similar issue(overboost)the small filter connected to the hose going to the stepping motor(solenoid)of the HKS was partially closed.
I just checked mine, very clean...
 
Old Dec 8, 2013 | 09:17 AM
  #40  
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I did a few hundreds km today, the engine is now >1200km, several short pulls in 3, 4 or 5 show 1.25Bar maxi, regulated.
I have to send some logs to Todd too.

The car is very pleasant and strong, but I want to be sure all is OK with the tune.
 
Old Dec 8, 2013 | 09:21 AM
  #41  
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Originally Posted by K24F
I did a few hundreds km today, the engine is now >1200km, several short pulls in 3, 4 or 5 show 1.25Bar maxi, regulated.
I have to send some logs to Todd too.

The car is very pleasant and strong, but I want to be sure all is OK with the tune.
Are you running flat boost setting or boost vs rpm or injectors signal?reset you ebc and recalibrate it.
 
Old Dec 8, 2013 | 09:28 AM
  #42  
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Originally Posted by dynamic gt2
Are you running flat boost setting or boost vs rpm or injectors signal?reset you ebc and recalibrate it.
EBC off for now
 
Old Dec 13, 2013 | 01:38 PM
  #43  
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I made several static tests, my solenoid seemed leaking, I worked on it and it seems ok now, but not sure until I run the car.
Tomorrow I will bypass it with a "T" , and will know the truth about my WG and my solenoid!
 
Old Dec 15, 2013 | 03:01 AM
  #44  
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Originally Posted by K24F
I made several static tests, my solenoid seemed leaking, I worked on it and it seems ok now, but not sure until I run the car.
Tomorrow I will bypass it with a "T" , and will know the truth about my WG and my solenoid!
Pascal,are you refering to the boost controller solenoid?"stepping motor"?when i am at full boost 1.5bar on 4th gear all windows closed i hear "pshpshpsh"this is the HKS ebc stepping motor"is it normal or leaking?
Thanks.
 
Old Dec 15, 2013 | 03:44 PM
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Originally Posted by dynamic gt2
Pascal,are you refering to the boost controller solenoid?"stepping motor"?when i am at full boost 1.5bar on 4th gear all windows closed i hear "pshpshpsh"this is the HKS ebc stepping motor"is it normal or leaking?
Thanks.
Normal IMO, you might hear the controled leak from the EBC to regulate the boost at it's target. (WG signal pressure is lowered, so the exceeding air goes in the atmosphere)

My today's tests demonstrate me my EBC is correct: even the solenoid bypassed with a simple "T" my effective boost exceeds the WG setting from about 0,3Bar, no leakage, all hoses new, zipped and well routed...
My conclusion is the Alpha's WG are a bit too small when they are used with a 3,8 kit and a real freeflow exhaust, and by winter with nice air density.
I finally setted mine to 0,9 and did some logs, sent to Todd.
The car is pretty strong, 100-200 in 5,5' with pumpgas, 2 persons in, but I need Todd's advice for the following...
 


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